|
|
|
After last
years mad rush of 60 to 80 hours per week, working on the boat to put
her back into a good, safe, cruising condition, we promised ourselves, not
again! This year we're going to slow down a little and finish
those items that, while still important, were lower on the to do list
and therefore didn't get done before we took off last year. And
this year, we're going to tackle them with minimal stress cause we've
got plenty of time to get our list finished before we head back south.
Reversing Gear - On our first 4,000 miles of
cruising we found that the reversing gear was slowly
leaking
oil from the seals and there was a delay between putting the boat in
gear and the prop starting to turn. Not a grave concern, as it was only a small
leak that we easily kept topped off and the delay was only about 3
seconds, but now that we're back state-side I pulled it out and took it to a good Volvo mechanic.
He took a good look at all the pieces and parts a pronounces them all in
good condition except for the cones, internal shift arm and seals. This job was fairly easy and painless
except for the cost of the Volvo parts. The parts were $900, the
labor $200. But the gear works great now! We also replaced
the cooling system hoses running to the gear and steam cleaned the
engine and ran a gallon of salt away through the raw water side of the
cooling system.
Spring Cleats - Last year I removed the WAY too
small, improperly installed, installed in the wrong
place, leaking like a sieve cleats that the former owner installed.
I didn't have the time to install new ones last year so I just
uninstalled them and repaired the damage. As I've said before when
talking about the former owners work...
"some people have no business working on their own boat!" Anyhow,
I located the cleats amidship where I could access the
underside
through the propane selenoid panel and an access port. I drilled
oversized holes for the cleats, filled them in with epoxy. Drilled
the hardened epoxy undersized and tapped them (this might be viewed as
excessive on my part, but it
only took a few extra minutes and I sure as heck shouldn't see any leaks
there in my lifetime!) for the 4' long 5/16 bolts. I then bedded the bolts
and cleats before screwing them in and securing them with Nylocks over
fender washers. Since I was using 4" long bolts that only showed
an inch below the teak and fiberglass deck/hull joint, I figured that
adding a 1/4 aluminum backing plate was probably WAY over-kill in this
location. Hmmmm...
Cabinet
hardware - This morning I had a couple of free hours before
work so I got out the Dremel Tool to fix some of the cabinet hardware
that just wasn't closing and latching as smoothly as we would like them
too. Nice! Now they're so Smmoooooth... I get points
for that don't I Deb??
Former Owner BS - Ahhhhh... first, another couple
fixes for a former idi... errr owner... install. Virtually every
little project that the former owner did was done using the wrong pieces
and parts or material. Usually it was stuff that he probably got
out of his garage like the bathtub caulk that he used to bed the
stanchions... Once again, I'm VERY thankful that he left all
of the big projects in the hands of professionals as apposed to tackling
them himself! I'm hoping that I'm getting close to having fixed
all of the former owners nifty little projects by now. The only
one that I know is left is replacing the WAY overpiched prop that he put
on... but that's for a story in Sept. when I haul Fat Chance.
The
first fix, was for something that I knew all along was a screw up, the
second, I had no clue until I traced the wiring...
The first was replacing a mild steel grease fitting that was installed
under the rudder packing gland. In the picture you can see the new
stainless one that I got from
McMasters-Carr for under $2.00. Now I only have to clean up
the melted mild steel one that's stuck to the bilge in the form of 5
foot long rust streak.
The second fix was a 110V outlet in the pantry that wasn't working (no
big deal, I didn't have time to fix it last year but I didn't really
need it either.) I have my wireless printer in the pantry and it
would be nice to have a way to power it therefore, the outlet was
perfect... Now... how come this outlet isn't working? First, there
were only 2 wires going to the outlet (which means no ground with AC)
and they weren't tinned so I removed them and finally discovered where
they were connected... can you guess??? The 12V buss bar...
nice... NOT! To save $8 the former owner is using the same
household style outlets and plugs for both his AC and DC! Amazing!
I'm surprised that this setup didn't kill someone or at the very least
start a fire. Folks, there IS a reason that you follow ABYC
guidelines and there IS a reason that you use marine grade parts and
pieces... If you're too cheap to do it right, you don't need to
own a boat! You risk your boat and peoples lives doing crap like
this! Sheeesh!
Re-bed
Port Lights - Not much to say here except that this is WAY easy!
You only have to remove the trim ring on the outside, clean out any
loose caulk and re-bed with your favorite Polyether or Life Caulk.
I used West
Marine's polyether because it flows so well that I was able
to get it WAY back in all of the gaps and cracks. As you can tell
from the picture, I didn't brighten or clean up the front of the trim
ring or the port. Maybe next year I'll tackle aesthetic
projects...
Freshwater Wash Down - While I was
down in the bilge to install a new holding tank, I decided to take care of the rats nest of fresh water hoses and
install a fresh water wash down system. Yes, I used hardware store
parts for my fresh water manafold. It's all schedule 40 plastic.
Firmly mounted there's almost no chance of it breaking BUT, if it did, it
would merely be an inconvenience and not life threatening! The bottom
valve drains the freshwater system for winterizing the boat. The
side valves lead to the watermaker's Flushing filter and the boats pressure
water system. The top valve leads to the new freshwater wash down pump and
hose, mounted in the top deck forward locker. Nice!
New
Holding Tank - Now for the fun projects!
I'm replacing the holding tank as the old Stainless tank's seams have started to leak.
I first looked at all of the stock roto-molded tanks.
Nothing.
Custom roto tanks cost 2K... I don't think so! I finally found a
company in Maine that does custom welded plastic holding tanks.
The prices are reasonable.
Triple M Plastic products
made me a new tank, to my specifications, and had it in my hand in less
than a week. It looked beautiful, all white and shiny . I
finally got around to the task of installing it because I had a chunk of
time (plus we need it now!) and it fit perfectly. With all new
hoses and a new vent fitting, all I needed to do was install the Scad
ultrasonic holding tank level indicator. The Scad monitor is an
easy install and has had very high reviews. When I finished wiring
the Scad up, I calibrated the empty tank level on the display.
Then I had to fill up the tank for the first time in order to calibrate
the full tank level. While I was finishing up the wire ties and
cleaning up below, Deb was pumping the the head to fill up the holding
tank with water. All of the sudden I hear the bilge pump
come on... hmmm... I didn't notice enough water in the bilge to activate
the
pump when I first came down here... I quickly checked all the
fittings to make sure that non were leaking... nope... The vent
hose is clear and empty. I finally looked at the bilge water and
saw a what appeared to be small flow lines coming from up forward and
out from underneath the tank... I had Deb stop pumping and the flow
appeared to stop... when she started pumping again, the flow lines
reappeared.... #^%@#! The tank must have a leak coming from one of
the bottom or rear welds is all that I can figure! I'm NOT happy!
Now I have to take everything apart again, including my water manifold,
get a new tank, get new ultrasonic sensors and redo all of what I've
already done... I don't need this! Not now. We need to
be able to use this tank today! I should have done this install
earlier on, I should have also put water in the tank before I
installed it, but I assumed (along with the "should haves" this one, I
shouldn't have!) that the company pressure tested the tank for leaks
before shipping. Who would have thought... I know better, I
always bitch about the former owner doing things on the cheap and here I
am, all because I didn't want to pay for a roto-mold or metal tank.
I'm going out to price welded aluminum tanks on Monday and will make
sure that the selected company pressure tests them for leaks BEFORE
shipping so that I don't have to do this again! This is NO fun!
Sheesh...
Note - After emailing Triple M Plastic, I received this explanation from
their president -
I am sorry to hear
that the tank has a leak. Contrary to your claim that we do not pressure
test our tanks for leaks before leaving here, we do. And we leave them
full overnight.
These tanks have a
weakness, and that is concussion. Should the tank be dropped during
shipping it is nearly impossible to see a crack if appears along a weld.
We will build you a
new tank free of charge, or refund your money, whichever makes you
happier. We have no control over how that tank is treated in shipping,
but I assure you that all our tanks are pressure tested before leaving
here. We have successfully been building tanks since 1972, and we are
truly sorry for this inconvenience. Please let us know how you wish to
proceed.
Almost September- OK, thanks to one
of the members on the Kadey Krogen Forum I was able to get a non custom
made, roto- molded tank from Ronco Plastics. This new tank
install was a pain because the tank was a few inches larger in every
direction. I had to remove deadwood from 3 sides plus some
glassed in wood that the old tank sat on. The total remove and
replace time was 10 hours, along with much cussing, but the job is now
done.
Injectors - No pictures here. I installed
new injectors and a new mechanical fuel pump as per last years mechanics
recommendation. In replacing the fuel pump I saw that the fuel
lines to and from the engines needed to be replaced. These are
both about 2 foot long, non pressurized 5/16 hoses. Guess how much
Volvo wanted for them... Can you say $150 each! I couldn't either
as I was sputtering too much... I will never own another Volvo.
Their parts are consistently 30% to 100% more than the same parts from
any other diesel manufacturer out there.
Bullet2HP
- I decided to upgrade my wifi from the 500mW Alfa client to Ubiquiti's
1000mW POE Bullet2 going down to a Linksys wireless router. I also
installed a mast extension to get the antenna a little higher and now
all is wonderful with the world. We now have strong wifi all
around the boat so were no longer required to sit at the desk with the
computer hooked to the Alfa unit. Very NICE!
The back porches' Teak Deck was in bad shape. The black seams and
underlayment had separated from the teak in so many areas that I was
starting to worry that water may start making it's way into the deck
core via the teak
decking
screws. While the teak looks nice and traditional, I don't have
the time, nor inclination, to pull up the teak, re-bed it, re-caulk the
seams, re-bung the screw holes etc. On my last trawler, Gecko, I
had the Vortex bed liner people come spray Vortex Urethane in a tan
color on the decks with good results. I was thinking of going this
route again when one of my friends told me about Durabak roll on
urethane. After seeing that it had the Navy and Armies approval I
decided to give it a try. I mixed 1 gallon of nonskid textured
cream with one gallon of smooth sand (color). I was able to apply
3 coats with a little bit left over (that had to be thrown away as the
stuff starts curing the moment that you open the can and expose it to
humid air). I think that I made the right choice. This is
really tough stuff! And even though we mixed half smooth, half
nonskid, the coating is excellent nonskid when wet. I'm very
impressed. While it doesn't look quite as nice as teak decking
did, it also doesn't let water through, cleans VERY easily and is
actually, a bit softer under foot. I now see
that Durabak comes in clear! Man... Oh well, that would have been
the PERFECT solution, waterproof, great nonskid and still looks like
teak... Oh well, at least the rest of you can profit from this info.
Teak Table - Today
I'm working on converting this teak table to as smaller convertible
coffee/dinning table. Wish me luck!

September 17, 2010
I wrote the above teak table line almost a month ago! When you're
busy, time
flies. Here it is mid September and I'm still not done
with all of the projects! I did get the table done and we're happy
with the results. I cut the legs off, trimmed a bit out of the
middle to narrow the table up, used Lock N' Pin seat pedestal for the
legs and
3/4" black Starboard for the base. The Lock N' Pins are
extremely sturdy, pretty sleek and allows us to convert the table from 20" coffee table height to
a 31" high dining table in about 30 seconds.
The use of expensive Starboard for the base was justified on 2 counts.
It's very heavy material making it perfect for use as a base for a
lighter teak top and, second it ties in to our saloon with the black
Starboard sliding cabinet doors.
I hauled the boat to put in a better
NMEA 2000 Intelliducer into the hull, change out my zincs, paint the
bottom (didn't need it but I was hauling so...) and finally try to determine the
size and pitch of the prop.
Bottom Paint - Last year I put 2 coats of West Marines CPP and PCA (50/50 mix)
ablative bottom paint on the hull after it had been peeled and reglassed.
Underneath that was an initial coat of West's Bottomshield epoxy bottom
paint that I used as a primer coat. When I hauled the boat it was
totally free of all growth except at the bottom of the keel where the is
no paint due to my exploring the shallows of the Bahamas. Very NICE performance for
such reasonably priced paints! I went ahead and put a couple more
coats on since the boat was hauled anyway. I should be good for a
few years now.
The prop... - ever since I bought the boat, I've known that the prop was
greatly over pitched. My top loaded rpm was 1100 under what Volvo
said that it should be for the TMD30A. Last year I couldn't find
any markings on the hub and when I called the former owner, he said
something like " don't you worry about the pitch! You got the
fastest Manatee, burning the least amount of fuel out there! It's
perfect!" Uhhh... no it's not! The experts (not my neighbor or the
other owners of Kadey Krogens), real experts such as Volvo engineers and
propeller specialists ALL say that to get the best performance
in both speed and fuel economy you need to match the prop size and pitch
so that you can reach the engine manufacturers max loaded rpm. I'm
no expert on this so I'm just quoting those experts that I've talked to
(remember that Kroganites)! The experts told me that people always associate
higher rpm with higher fuel consumption. Therefore they think that by overpitching their props and reducing their rpm's, that they're saving
fuel and going faster. All those same experts said
that this assumption is patently false! Apparently what dictates
fuel consumption even more than rpm, is load. By overpitching your
prop (yes even just a little!) you're overloading your engine from the
time you put it in gear right up through the, now lower, top end of the
power curve. This is hard on the engine, reversing gear, shaft
coupler (the former owner replaced 2) and it consumes more fuel! Please,
save the hate mail for the experts that I'm quoting. As I stated
above, I'm NOT an expert in this field and hence I'm relying on and
quoting real
expert.
Anyway... after brushing down the bronze prop I finally found the size
and pitch marking and with some ink tricks was barely able to make out the 22x16.
3 inches overpitched from the 22x13 that the Manatees come with from the
factory and 4" overpitched based on a 90hp Volvo and a cruising
displacement weight. I have a new prop coming from Ron at
Wolverine Propellers.
It's a Michigan Wheels mp (machine pitch) 22x12. Ron will refine
the prop to within thousands of an inch and tune and balance the prop
before sending it to me. You pay msrp for the prop that you buy
from Ron, but everything else is included as a free customer service.
Ron is very competent engineer that actually listens to his customers
and then tries to guide them to a prop that will work best for their
needs and therefore make them happy. I haven't experienced
the customer service and support that I got from Ron in some time.
Thanks Ron! And for the nay sayers at the Krogen owners group, if
Volvo, Michigan Wheels, Boat Diesels, Wolverine and Deep Blue, as well
as the many pitch calculators that I used (all of the calculators
figured 22x10 or 22x11) are wrong, it's simple and cheap to increase the
pitch by an inch. Right now though, I'll go with the experts...
12/5/10 - And am I glad that I did!
Even this prop is a hair overpitched! I do mean a hair. In
calm waters I do 7.5kts
@ 3000 rpm, 8.0kts @ 3300 rpm and 8.5kts @ 3600 rpm. I top out at 3700
rpm with no gains in speed. Volvo specs say you should top out at
3800 rpm under load with correct prop, but hey, this is close enough for
me and WAY closer than the 2700rpm that the last prop would allow the
engine to top out! The engines reversing gear doesn't clunk when being put
into gear anymore. The 120 amp Balmar alternator is happier
with a few hundred more rpm and I
actually have better control of the boat when docking. The big
question, yet to be answered, is fuel consumption. I'll post the Fuel #'s when I get some good
ones. I tried to fuel up in NC but had problems due to mud daubers
clogging the fuel vent so I won't be able get a Beaufort to Ft. Pierce
#. ****Fuel #s -with the old prop (overpitched) I went slow so as
to not stress the engine. So my average fuel consumption was
running at 6 to 6.5 kts and burned 1.9 gal/hr, my 7 to 7.5 kts with that
same prop burned an average of 2.7 gal/hr. With the new prop I've
been happy to run the boat at 7.5 kts average because I knew that I
wasn't stressing the engine. My initial average fuel consumption
at that speed is 2.45 gal/hr. So my feeling is that I'm burning a
little less fuel with the properly sized prop doing much higher rpm's...
I'm certainly not burning more... So the experts are right...
imagine that. 3/5/11 - I just filled up in George Town, Exuma and
my fuel consumption since filling in Nassau has been 1.91gal/hr.
My average speed was probably a little lower than 7.5kts when you figure
in all of the slower motoring into anchorages. Still tickled with
having the properly sized prop! No down sides at all!
Solar Panels - I've been putting this job off,
both so that I could think about different ways to do it and because I
know that it will be a bitch no matter how I go about it. I want
to put the solar panels on the pilot house roof, out of site, out of
mind and out of danger. But the roof is a hollow
fiberglass
structure of which the top half has caved in about 1.5 inches and attached itself
to the bottom half. I have to find some way to pry the 2 halves
apart and make the roof structurally sound. In my research, I
found that there was no way to get a 2 part high density foam (8lb)
poured in place and have it flow throughout the structure before curing
(60-90 seconds). So I decided to cut the roof open, along the
edges, where I will be glassing in some lumber to attach the framework
for the panels.
This made using a 6 foot long piece of flat steel, to separate the 2
halves, WAY easy (If you can call 6 hours of pushing steel easy...).
With the fiberglass separated I'm going to install treated 1x4s, with a
slight crown, approximately every 16". I'm
then foaming the rest of the cavity with a low density 2 part foam spray
kit, fiber glassing over the
openings and and repainting the roof with my
new favorite coating, Durabak.
I'll then install 2 SS support posts that I'm having welded and
polished, one of which is hollow to act as a wire
chase, run the cables from the roof down to the batteries, install a
regulator and breakers along the way, attach the solar panels to the frame and mount the frame
on the pilot house roof...
That's the plan anyway! Piece of cake huh?
Wrong! What a PAIN this little project was!!!! This one has
fought me from start to finish! It has taken about 4 times a long
as I planned and has cost... well what do you know... exactly what I
thought it would cost... What can I say but, "give a monkey a
bowling ball and every now and then, he's gonna get a strike."
After prying the fiberglass panels apart, I cut some 1x4 to lift the top
fiberglass panel
and give it the proper crown for good water run-off and extra strength.
I then used a low density, 2 part, spray foam kit to fill the air pocket
between the fiberglass. Unfortunately, because I believed what I
was told by the company selling me the foam, I had 2 problems that
left
me with less than a perfect job. First, the foam was
supposed to be totally expanded and mostly cured within 90 seconds and
therefore allowing for a slow fill without overexpansion and
"bubbling", wrong! Even injecting the foam slowly, to allow all of
the expansion to fill the empty void as apposed to pushing up on the top
panel, didn't work well. Several areas kept expanding well after
90 seconds even though the temperature was at the optimal recommended
level. The result was a finished roof, that, while strong, is
somewhat lumpy.
Second, and even worse, "the foam is so easy to control that there's no
reason to cover the rest of the boat," wrong again! Yup, the foam
was easy to control, but the spray tip securing mechanism was not strong
enough to hold the tip on. When it popped off, it spattered
the side deck. Duck tape kept that from happening again but the
damage was done...
Before the slots cut on each side of the roof were fiberglassed, a
treated, dry, 2x4 was inserted
and
held flush with the top. Polyester resin was then poured
underneath to support them. The roof was then finished with 2
coats of white Durabak. While I was finishing up the roof my metal
guys were making me 2 stainless support posts. These were not
necessary for support, but we wanted them to use as handholds when
moving around offshore and one would
make the perfect conduit for running the 2 sets of #6 cable from the
roof top down to underneath the pilot house seats. The cables then
went down through the head before hooking up to the Blue Sky Solar Boost
50 (with Maximum Power Point Tracking (MPPT) technology) regulator and
the batteries. I also installed a remote panel for the Solar Boost
in order to be able to monitor the system.
The
easy part off this project was assembling the 2 arrays of 4 - 85W
panels. After a bit of research, I settled on 8 - 85W panels.
As apposed to 3
- larger wattage panels, the losses due to panel shading by the mast and
radome, are minimized with the smaller panels. These panels are
light and easy to handle. Putting the arrays on the roof and
wiring them to the cabling going to the batteries was a 3 person, half
hour job.
While
doing all of this I also found time to install a wind generator,
increase my battery bank and replace all of my batteries. Whew!
If we weren't such energy pigs I wouldn't have had to
do...

All of the Electronic parts and pieces, including the solar panels, wind generator,
MPPT regulator came bundled from the nice guys at
eMarine in
Ft. Lauderdale. They made sure that I not only had the right gear
for my needs but that I had all of the little incidentals that make putting it
all together that much easier. They sell the best products
and better than that, they stand behind them! I don't get to say
it enough so... eMarine... Thanks!
Propeller - Next, I'll be testing the new prop out.
Cast by Michigan Propellers and Tuned and balanced by Ron at Wolverine
Propellers. I just painted it with Propspeed and am waiting on
getting a quick haul to install it. Results are posted in Red
above where I go on my diatribe about fellow cruisers thinking that over pitching
a prop is a good thing...
Hinges
- Well, since the last update, I finally finished the last
big jobs and a bevy of smaller jobs that won't be posted. After
searching the world (literally!) for matching hinges for the rear
door/swim platform I finally had a local welder make me a custom set
that would guarantee that they'd fit and be strong enough.
Only $65 per hinge! Oh well, they fit perfectly and are strong so
now the door works again!
Teak Trim - "What! You painted the
teak trim!!! Are you crazy!!" Nope, I'm not. After
almost 30 years of keeping teak bright, I'm over it. We first
sealed the teak with Interlux wood sealer so that if some future owner wants
to take the teak back down to where it can be varnished,
he
can do so without too much fuss. We then painted the teak with
Brightside single part urethane paint in the "Sundown Buff"
color. We love it! Looks great to us and we shouldn't have to do more than touch
it up here and there as needed for the next 7 or so years! That
gives us weeks of extra time to enjoy life every year cause we won't be
spending it keeping up teak. Yeah! Time to go cruising!
Enjoy!
Please note, when I mention the "former owner" on
these Projects pages, it refers only to any, all or non of the real
former owners, there associates, friends or mechanics that had a hand in
doing whatever " bad or stupidly done repair" that I'm bitching about at
the time.
|